bvolcko38 wrote:Bryan,
What kind of borescope do you have?
Bill, something Adam got on Amazon for $70. It's chinese, has a forward & side camera. It works well enough!
kmacht wrote:That valve doesn’t look too bad. I would triple check to make sure your rockers have the correct .004-.006 gap as being just a little off can cause the valve to open early or late and mess with compression measurements. It’s very common for that measurement to move around for a while after a rebuild.
Keith,
That valve was cooked. It is a little easier to see when you are moving the camera around than in the static picture. We could see a gap. Also we did check & set all the valves. The #1 exhaust was at 0.005", and my manual says 0.006-0.008. We reset it to 0.007. But besides the picture and the 80/13 leakdown, there is this:
1) Very low compression when turning over by hand
2) With the leakdown test going, you could easily move the prop around off TDC and it didn't want to take off like a normal engine.
3) With the leakdown test going, air was pouring out the exhaust pipe.
4) We moved the prop around to open the valves and look at the seats. They were horrible. It was clear they were not sealing well.