daleandee wrote:sonex1374 wrote:Dale,
The damage to the turbo was caused by the crash impact forces, and only after the crash the turbo wouldn't rotate. The investigation notes and pictures of the turbo show that the damage to the housing was caused by the impeller wheel impacting it during the crash. The turbo would not rotate simply because it was damaged in the crash! The rest of the investigation showed no pre-impact turbo anomalies. The NTSB report could have been much better here, and Joe is trying to clear up any misunderstandings.
I see you edited your original to make it nicer. I appreciate that.
For everyone concerned I'm gonna leave this alone as it's apparent that regardless of the facts of the NTSB report (trust me there are more concerning questions I have) there seems to be a great resistance to acually reading the NTSB report and speaking to what is there.
No doubt an answer won't be found but when the well known, long time members of this community start professing truths that are contrary to the stated facts of the report ... I'm done. I refuse to seek answers from those that aren't willing to search for them.
Dale
N319WF
kmacht wrote:Was the finger strainer in the tank looked at during the investigation?
kmacht wrote:Any contamination at all found in the fuel tank?
kmacht wrote:Did it have a gascolator or a fuel filter?
kmacht wrote:Second, what type of mixture control was installed. Was it a push button lock or friction lock?
kmacht wrote:Finally, was the position of the aero carb needle confirmed to be close to where it should be?
andrewp wrote:And thank you for teaching me how to land my Sonex before I had flown it. I had a really awesome time back in 2013 and I know you have helped a lot of others since then (actually I think I was the t-flight practice guy? ... whatever I enjoyed the heck out of it).
Hello Jason,
I would like to formally object to the statement in the report’s “Analysis” section -- paragraph 2, sentence 5: “It could not be determined whether the turbocharger would not rotate due to impact damage or whether it seized in flight resulting in a partial loss of engine power.”
According to statements by Joe Norris, he reports that, with your oversight when examining the turbocharger before it was sent to the NTSB laboratory, the impact damaged portion of the turbocharger housing was removed, and the turbine shaft was found to be rotating freely once pressure from the impact-damaged section was removed from the turbine. Joe’s account of the initial turbocharger examination directly conflicts with the statement in Factual Report section “Wreckage and Impact Information” paragraph 5, stating that disassembly was halted after finding a crack in the housing, and this bears clarification. I’ve copied Joe on this email and would like for you both to communicate about the actual sequence of events.
Factual Report section “Tests and Research” paragraph 2 also states that “Both the compressor wheel and turbine wheel turned together freely within the center housing when either was rotated by hand.” This statement also conflicts with the mischaracterization of the “Analysis” section of the report, paragraph 2, sentence 5 as quoted above.
What is our process for clearing these items up in the report?
Thanks,
-Mark
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