kmwoody wrote:What did they know that they didn't want the paying customer to know?
Ken W
kmwoody wrote: What did they know that they didn't want the paying customer to know?
daleandee wrote:1) The surveillance video of the flight showed what the investigator called "white smoke" appearing a couple of times from the aircraft. They tried to duplicate this with fuel changes and even water. Did they consider that this had to be oil burning as it is light blue and would appear nearly white?
daleandee wrote: There was a cracked bearing housing found in the turbo. There is no way for them to know if this was a pre or post impact crack.
daleandee wrote:Could it be that the turbo was cracked and the smoke was seen because of oil entering the turbo and being burnt? Could this be the cause for a turbo seizure and power loss? Power output without a turbo would be very low considering the restriction and the large prop for the 100 hp set-up.
daleandee wrote:3) How many passegers had been flown in this aircraft?
daleandee wrote: Did the factory do any gross weight testing with the turbo installed?
daleandee wrote: How many passengers did Jeremy himself fly in this aircraft or was Mike his first passenger?
daleandee wrote:There is no question that this has been very difficult for those much closer to him & Mike than we are. Keep this in mind and please remember these in your prayers.
Sonerai13 wrote:This was discussed during the investigation. Nothing that was found would indicate that there were any oil leaks of any kind in or on the turbo.
Sonerai13 wrote:There were no pre-existing cracks of any kind.
Sonerai13 wrote:Again, as I have stated earlier in this thread, there was no evidence of a turbo seizure, either partial or full. I verified this personally during the investigation.
Sonerai13 wrote:That is incorrect. The airplane had recently returned from a 25 hour cross-country to Florida and back. The engine had considerably more time on it than that, first in the test cell and then on the airframe. I personally witnessed all the testing on this engine, and I flew the cross-country to Florida and back. The engine performed flawlessly throughout the entire program.
Sonex Sport Acro N123SX first flew in 2007, and has most-recently been fitted with the 100 hp AeroVee Turbo. The engine had accumulated approximately 25 hours of operation in the Sonex Aircraft test cell as part of the AeroVee Turbo development program, and approximately 50 flight hours on N123SX after moving from the test cell to the Sport Acro airframe in the spring of 2014.
daleandee wrote:Sonerai13 wrote:There were no pre-existing cracks of any kind.
Call me ignorant but I'm not believing that. There is just no way that they could know that after the fact.
daleandee wrote:Sonerai13 wrote:Again, as I have stated earlier in this thread, there was no evidence of a turbo seizure, either partial or full. I verified this personally during the investigation.
That's not what the report says. It says clearly, more than once, that the turbo would not turn and that there was no evidence that it was turning at the time of impact.
daleandee wrote:Many of us are quite disappointed with this investigation. Not because it didn't render an answer so much as because there were a few other roads that were not followed that should have been.
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