by fastj22 » Sat Dec 05, 2015 7:16 pm
My experience with MGL RDACs and using the alternator pulse for RPM pickup is problematic.
It seems to be very susceptible to noise. My first RDAC, a XD, worked fine from an RPM range of 0 - 1300, was jumpy 1300-2000 and stable from 2000 up.
The XD failed this fall and I replaced it with an XF. Now RPM is stable from 0 - 2500, but goes nuts above 2600. I've tried lots of setting adjustments, per MGL. Also have been fighting other sender issues that generally get solved by grounding everything to the engine, not the firewall.
If you guys figure out the perfect settings, please publish them.
John Gillis
SEL Private, Comm Glider, Tow pilot (Pawnee Driver)
Waiex N116YX, Jabiru 3300, Tail dragger,
First flight, 3/16/2013. 403 hours and climbing.
Home: CO15. KOSH x 5
Flying a B-Model Conversion (Super Bee Baby!)