by n502pd » Sun Aug 11, 2019 6:40 pm
Maybe an old subject, but I have had in the last several hours, another incident of very high oil pressure.
I had landed after an uneventful 30 min flight after condition inspection, shut down, chatted with airport bums for about ten mins, restarted with some difficulty (probably heat soaked fuel supply as this was the first time I had stopped for such a short time), and taxied to runup and take off again. Durring initial stages of run up, oil pressure began to climb well above of 100 psi. I aborted and returned to hanger.
After cooling with a fan, I investigated pressure plunger/pistons,valves. Rear one was good as it slid right out, and wasnt stuck. However the front was different. It need to be coaxed out with a wooden dowel. I found very small particle in the bore when cleaned. Not aluminum and not steel, so I dont know what it was. Opened the oil filter...nothing inside...changed oil...again nothing.
Here is what I surmised. the spring end under the piston...not on the silver plug that is screwed into the block...sits on the bottom of the plunger in the top of the block bore, and is not centered in the bore because the bottom of the piston has a curved surface where the spring coil contacts the piston. Since the spring isnt captured on bore centerline by the piston, the top coil of the spring is free to move latterally in the bore and will contact the surface of the bore. That contact can, and appairently has, scuffed off small parts of the bore surface, and has caused the piston to hang, thereby causing higher than normal pressure. I suspose low oil pressure might be caused by the same senario, but I have not seen that personally.
So my questions here are, how many others have run across this pressure malfunction? And, what have you done about fixing it so as to not happen again, other than the careful polishing of the piston? Further, has anyone actually discovered bore particles from the cleaning of the bore, or marks in the bore, as I have on my first happening with the rear regulator piston,and again on the front piston, and what was the fix? Did the fix last? The first time was at 17 hrs tt, and the 2nd was at 30 hrs tt. Using Valvolene 20-50 vr1, and fram hp3 filter, changing at 25 hrs. Nominal press 62-70 psi hot, max temp seen 190 or so.
Thanks for any input!
Joe
Joe Nelsen
scratch built :D
Sirpeedee, N502PD, s/n 1510, Aero Vee 2.1 s/n 0870,
ADS-B in (Stratux)/out(SkyBeacon)
Flying @81.7
KGYI/N. Tx Reg/Perrin Field
EAA Technical Counselor, Chapter 323, Sherman, TX