by Nqsonex » Sun Oct 28, 2012 6:16 pm
Hi mike
Yes definitely glad to get it down in one piece.
As for temps they were all still in the green, the outside temp was approx 31c, and about 90% humidity, both egt,s and cht,s were under max, the height attained was only 2500ft, also leaning was tried but only made the situation worse.
The carby had been tuned for summer recently and until now had been running fine, this is the first longer run for the summer months, it has done about 20 hrs over the last 2 months.
As for the fuel plumbing there is an exposed alloy pipe that exits the firewall on the pilots side and runs across the firewall to the exposed gascolator then to the aerocarb, it is now going to be rerouted and fire sleeved to see if this helps.
The plane hasn't,t been flown as yet, only found testing has been done and all seems fine, no issues under any load up to full power.
Will keep you all posted, just an issue we don,t wish to see again for obvious reasons, to date the aircraft has done approx 140 hrs total, mainly in the cooler times of year.
Cheers