Got the engine running for the first time since I took over the project.
Curtis Valve on the gascolator leaked so bad it was leaning out the carb, which I've been tweaking per Jeff Schultz's suggestions
http://www.sonex604.com/aerocarb_thoughts.htmlFinally got the brakes bled, and they work GREAT. I love the parking brake valve.
Just like the previous toilers on this project, I could NOT get the magnetron ignition to work, and I'm pulling it off to replace it with a Simple Digital System Coil Pack ignition. I've started to work up the bracketry I'll need to mount the Hall Effect sensors for the crank trigger. I've been planning this since BEFORE I bought the project, but wanted to give the Magnetrons ONE MORE CHANCE, and they failed.
Progress and pictures at
http://eaabuilderslog.org/?s=wlawrence The FAA paperwork for Certification is mocked up, but I'm waiting to get my medical Special Issuance back before I fire it off, plus I need to finish the Weight and Balance, so inspection and first flight are looking like September/October of this year.